HomeMy WebLinkAbout15- Engineering Report Letter[50]Professional Consulting Engineers and Land Surveyors
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Engineering Report:
for
705 S Church Ave.
Bozeman, Montana
August, 2025
Prepared For:
Landern West LLC
Prepared By:
Hyalite Engineers, PLLC
Brett Megaard, PE
705 S CHURCH AVE
ENGINEERING REPORT AUGUST 2025
1. Project Information
The property is approximately 1.4 acres located at 705 South Church Ave in Bozeman in the
southwest quarter of the southeast quarter of Section 7, Township 2S, Range 6E in Gallatin
County, Montana. The property is within the City of Bozeman city limits. Currently the property has
an existing house which is serviced by a drainfield (permit no. 05109) and a city water service. The
property has a 6” clay sewer main that runs along South Church Street to the east and across
Bozeman Creek to the west an 8” clay sewer main and manhole that runs on the western edge of
the property. The owner is seeking approval to connect a townhouse with nine (9) bedrooms total
to the city sewer system. Currently the sanitary sewer main that runs along South Church does not
have the capacity to service the proposed residence. However, the existing sewer main and
manhole on the western edge of the property as mentioned above has capacity. The proposed
connection to the city’s sewer system will consist of a septic tank outside the townhouse that will
discharge to a E-one pump station. Once the effluent reaches the pump station it will be pumped to
an existing 8” clay sewer main approximately 274 feet away, this will also require that the
transmission line from the effluent pump to be bored and sleeved underneath Bozeman Creek. A
4” inserta tee is proposed to be inserted into the existing 8” clay main. Extending from this inserta
tee will be approximately 21 feet of 4” SDR 26 sewer service line that will connect to the 1.5”
transmission line. This connection to the western sewer main would serve as a temporary option
until the S Church City sewer main is upgraded to accommodate the flow. This private service
connection is to be privately maintained.
2. Water Supply and Wells
The existing house on site is connected to city water and this service is proposed to be abandoned
at the main per City of Bozeman Standards. The proposed new townhouse will also be connected
to city water with one water service.
There is an abandoned well on the property however it is no longer in use. The closest neighboring
well is to the south and is more than 100’ from the property boundary. No other wells are known to
exist within 100’ of the subject property as the neighbors to the North & South are both currently on
City water & sewer.
3. Wastewater Design Flow
The proposed building will contain 2-units. Unit A will be 4-bedrooms (350 GPD) and unit B will be
5-bedrooms (400 GPD). The wastewater design flow for the proposed 2-unit residence is 750 GPD
(350 GPD + 400 GPD). Calculations were based on MDEQ Circular 4, Chapter 3 Regulations.
Maximum Day Flow
Peaking factor = 2.3 (per City of Bozeman Design Standards)
750 gpd (2.3) = 1,725 gpd
Max day flow = 1,725 gpd / 1,440 = 1.20 gpm
Peak Hour Demand
Peaking factor = 3.0 (per City of Bozeman Design Standards)
750 gpd (3.0) = 2,250 gpd
Peak hour flow = 2,250 gpd
2,250 gpd / 1,440 = 1.56 gpm
Design Peak Instantaneous Flow
Peaking Factor = 10
750 gpd (10) = 7,500 gpd
705 S CHURCH AVE
ENGINEERING REPORT AUGUST 2025
Peak instantaneous flow = 7,500 gpd
7,500 gpd / 1,440 = 5.2 gpm
4. Septic Tanks
There is currently one septic tank that serves the existing residence which will be removed. The
proposed residence will have a new 4,000-gallon septic tank and E-one grinder pump station. The
sizing of the septic tank was based on MDEQ Circular 4, Chapter 5 for 2 units (A & B) with four (4)
and five (5) bedrooms. The proposed tanks are to be reinforced concrete, non-traffic rated. The E-
one pump station will have two (2) submersible grinder pump that will pump effluent to the existing
manhole.
The septic tank is to be manufactured by Three Fork Precast and shall be watertight. All tanks
located in high groundwater areas shall have a water leakage test performed and concrete additive
for water proofing (or approved equal). A vent is to be connected to the pump station with a carbon
filter. The septic tank and pump station are both located outside of the 100-year floodplain of
Bozeman Creek. Buoyancy calculations were checked to make sure the weight of the septic tank,
pump station and soil were more than the upward force due to buoyancy. The groundwater depth
can be as high as 4.5-6 feet during the spring months. The buoyancy calculations are below:
Pump station
Volume of liquid displaced = 22x3.14*7.5’ (depth) = 94.25 cubic feet
Force of Buoyancy = 62.4 lbf/cubic foot x 94.25 cubic feet = 5881 lbs
Weight of Pump station =
Concrete collar around pump station base 12” thick = 7.06 x 145 lb/cubic foot =1,024 lb
Total =1,024 lb
Assuming groundwater at 2 feet.
Soil Bearing Weight on pump station = 56.55 x 110lb/cubic ft (soil weight) – 21.2 x 62.4lb/cubic ft
(water weight) = 4,898 lb
Total weight = 5,922 lbs
Septic tank
Volume of liquid displaced = 8.17’x16.42’x6.58’ (depth) = 883 cubic feet
Force of Buoyancy = 62.4 lbf/cubic foot x 883 cubic feet = 5,508 lbs
Weight of Pump station =
(2 walls) = 15.58’x0.42’x5.74’x145 lb/cubic foot x 2 (walls) = 10,893 lb
(2 walls) = 7.33’x0.42’x5.74’x145 lb/cubic foot x 2 (walls) = 5,125 lb
(bottom) = 16.42’x0.42’x8.17’x145 lb/cubic foot = 8,170 lb
(lid) = 16.42’x0.42’x8.17’x145 lb/cubic foot = 8,170 lb
Total = 32,358 lb
Assuming groundwater at 2 feet.
Soil Bearing Weight on pump station = 8.17’ x 16.42’ x 3.5’ x 110lb/cubic ft (soil weight) – 8.17’ x
16.42’ x 1.5’ x 62.4lb/cubic ft (water weight) = 39,092 lb
Total weight =71,450 lbs
705 S CHURCH AVE
ENGINEERING REPORT AUGUST 2025
The unit weight of the concrete and soil bearing for both the pump station and the septic tank is
more than the upward force due to buoyancy, so the pump station will not try to float.
5. Manhole Location and Force Main
As mentioned above the owner is proposing to connect to the existing sewer main that is on the far
west end of the property. Currently there are 8” vitrified clay mains that come in and out of a
manhole that is located on the property. The existing gravity sewer mains have been sized to meet
the minimum standard by the City of Bozeman, as an 8” sewer main at the minimum of 0.4% slope,
can handle approximately 314 gpm. With an average daily flow of 0.52 gpm produced from the
residence this is a very minimal impact to the current system. The peak instantaneous flow
calculated above has minimal impact on the City’s system with a gpm of 5.2.
It is proposed that the force main be 1.5” diameter DR 9 HDPE from the pump station to the
existing sewer main. This force main connection to the city will require it to cross Bozeman Creek.
The force main will be directionally drilled and sleeved as close to perpendicular to Bozeman
Creek as allowed in order to tie into the existing gravity sewer system. The proposed bore and
sleeve will be located outside of the floodplain of Bozeman Creek. The design of the force main
was based on MDEQ Circular 2 Chapter 49. Once the effluent has left the force main/transmission
line it will gravity flow to the City of Bozeman’s wastewater treatment facility.
To maintain a 2 ft/s minimum velocity per DEQ Circular 2 Chapter 49 a design flow of 10.4 gpm is
needed to achieve the 2 ft/s. The proposed design flow of the E-one grinder pump is to be 14.3
gpm. Using a pump curve for E-one’s SPD grinder pump and Orenco Pump Select program to find
total head loss and the design flow. Leakage testing will be completed on all portions of the sewer
force main in accordance with the same testing procedures for water mains and in accordance with
the MPWSS. In addition to testing the force main is proposed to have antiphon, shut off valve and
check valve as it leaves the pump station.
The proposed bore and sleeve under Bozeman Creek is to be 6.5’ from the bottom of the creek to
maintain adequate cover for forced mains. BMP’s will be used where necessary, however
adequate separation will be included for the directional drilling in order to ensure no siltation or
erosion occurs near or in the stream/streambank.
6. System Specifications
The Orenco Systems Pump-select software was used to determine the pipes, flow rate, and total
dynamic head of the proposed systems.
The transport pipe to the drainfield is to be 1.5 in dia. DR 9 HDPE. The transport pipe is to be
approximately 274 feet to the proposed sewer service line that connects to the existing sewer
main. An E-one grinder pump was determined to be adequate for the system. The proposed pump
station will have 2 (two) E-one grinder pumps within the pump station. The alarm system is located
on the control panel which is to be mounted on the proposed building.
The dose volume for the proposed townhouse residence supplied by E-one and is to be 31 gallons
per cycle, which is greater than the volume of the transport line. The E-one pump station holds
7.75 gal. per inch. The distance between the “off float” and the “on” float is to be 4 inches, allowing
for a true dose volume of 31 gal. According to E-one this pump is designed to run frequently
hence the low dose volume. The reserve required by MDEQ is 25% of the daily flow rate of 750
gpd. This is equal to 187.5 gal. or 24 inches. A E-one grinder pump requires at least 13” of
705 S CHURCH AVE
ENGINEERING REPORT AUGUST 2025
submersion, based on this criterion the low-water redundant off switch is to be positioned at 13”.
The floats monitoring the dose pump switches are to be set at the following elevations according to
E-one design parameters (inches from the bottom of the tank):
Hi-water alarm - 25”
“On” - 17”
“Off” - 13”