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HomeMy WebLinkAboutPHASE I & II INSPECTOR'S DIARY t w t_ 1Liston lamn . vey w WEEKLY REPORT W .O . # 86 -511 -1 Lyman Creek Water Systems Improvements June 19 Through June 23 , 1989 NELCON , Inc . worked for four days this week June 19 through June 22 , 1989 . The 4 " D . I . P . drain lines for the pressure reducing vaults were excavated , installed and backfilled along with the drain outlet structures at Sta . 23+00 and Sta . 52+00 . All necessary pipe , valves , gate valves , butterfly valves ; couplings , bends , tees , and reducers were installed to connect the existing 18" water line , by pass structure , and control valve vault . The interior valves , bends and piping for the pipe gallery have not been installed . The reservoir outlet control structure was excavated and placed . The existing 12 " reservoir outlet and the existing 10 " drain down pipe were found and excavated . Two inch minus gravel was hauled and placed on the access road . Vogel Construction Co . placed the 8 inch concrete block for the chlorine building on Thursday . No work was performed on Friday , June 23 . Gaston: loy 'ct� yF.. 'f21; ip WEEKLY REPORT W.O. # 86-511-1 LYMAN CREEK WATER SYSTEMS IMPROVEMENTS June 12 through June 16, 1989 Nelcon, Inc . worked four days this week , June 12 through June 15 , 1989 . All the valves , spools tees , bends , reducers , and adap- ters were installed in the pressure reducing valts at Sta. -23+00 and Sta. 52+00. Ten bentonite cut-off walls were excavated and the bentonite and soil were mixed , placed and compacted. The Pipe Gallery and Inlet Control Structure were excavated and the precast concrete structures placed and backfilled. Jefferson Valley Construction Co. formed, tied the steel, placed and finished the concrete slab for the chlorine building . Surface restoration of "the pioneered road from Sta 0+00 to 19+00 was completed and seeded . Two inch minus gravel was hauled and spread on the access road from Sta. 19+00 to Sta. 38+00 and Sta . 46+00 and to Sta. 52+00. No work was done on Friday June 16. Julian Dodge '.., :� 1Z h L 1 f1 `1 L n « ;l ;3r 'I. i � �h ,;r. �', •ni,u�. NIT .GI: .ii„i ..Yi .�� ti;i, ;u� i'_.,.,. 1' ,L.i❑ .. r.-. . •i l � r. _. �. t�"i ti.. d _ W . O . # 86-511 LYMAN CREEK WATER SYSTEMS IMPROVEMENTS June 12 , 1989 Mr . Glen Stensrud Nelcon Inc . It has come to the attention of this office that subcontractors of Nelcon Inc . working on the Lyman Creek water systems improvements for the city of Bozeman have been using excessive speed . The location in question is the access road to the project site that crosses North Hills Ranch . Proprietors of North Hills Ranch have made compaints and as a result of this , the City of Bozeman has installed 15 m . p . h . speed limit signs on either end of the road . We would like you to inform all your employees and subcontractors to comply with the posted speed limit . Julian Dodge O i: i 1 it t7 r 'l 1 1 t' C' ! i C Z _ E'O B.. 4h1, _`'il \. ill A.0 . 3,v�1;1:111. \1i- � 4 v l * ' }4a L WEEKLY REPORT W.O. #86-511-1 LYMAN CREEK WATER SYSTEMS IMPROVEMENTS June 5 through June 9, 1989 NELCON INC. worked four days this week June 5-8 and per- formed the following. Thrust blocks were poured on the remaining 221° and 450 bends , tees , and the plug. For the pressure reducing valts the two areas at Sta. 23 + 00 and Sta . 52 + 00 were excavated , bedding placed and precast concrete valts placed. The reservoir and dike near Sta. 61 + 00 was excavated and built . The diversion structure near 61 + 00 was installed and connected to the 16" x 16" x 16" tee with 20 ' of pipe and two 2210 bends . Also the 30" C.M.P. was installed to the diversion structure . The 16" D .I .P. drain down line was placed with a 16" butterfly valve and box. Near Sta. 60 + 00 area the air relief valve manhole was installed with the 6" D.I .P. connected to the 16" x 16" x 6" tee and gate valve. The footings and foundation wall under the front and both sides of the concrete walk for the chlorine building were formed, steel tied and concrete poured . Reclaimation of the pioneered road from sta. 0 + 00 to sta. 17 + 00 was performed. No work was done on Friday June 9. Julian Dodge n > U Y_' L ' li C.l S) +� ;3, >t•i _�':i � '.h ',c�., i: ..ai_n. � i. _,rj b ,.,;ti tiil„ .,,_r _. Al .v;i�.. .. .ii _. S f_ Gaston -j1-En ,, Surveying E G� W.O. #86-511-1 LYMAN CREEK WATER SYSTEMS IMPROVEMENTS May 29 through June 3 This week Nelcon Inc . installed 1, 677 L.F . of 16" D .I .P water line from Station 54 60 to Station 38 40. Nine 111 bends , two 222 bends , and two 45 bends we-re mechanically attached to the 16" water line . Trench backfill was placed and compacted except over the 222 bends that still need thrust blocks . On friday May 26, the foundation walls for the chlorine building for formed and concrete placed. Monday May 29, no work was done due to the holiday. Two gates were installed on June 3, the area from Station 0 00 to Station 17 00 will be worked on to bring back to a natural state . Gonsu ? yin ; En - i neers Lk La—Ind S ors * . P.O. Boy 9Oi. 2010 N. -th -%ve.. Ho,%:rmn. NtT 5(17-15 Slkel- 80M (',nfcr. 125A. Granite. BU11Q. '.1'l' �0701 t hi :-1u3 t� Survoying y WEEKLY REPORT W.O. #86-51.1-1 LYMAN CREEK WATER SYSTEM IMPROVEMENTS May 30, 1989 It has been brought to my attention by Glen Stensrud , superinten- dent for Nelcon. , that a horse owned by North Hills Ranch was destroyed this morning following an injury sustained over the pre- ceeding weekend. Glen Stensrud discussed the incident with Mrs . Rugheimer this morning and reported the following . The injury to the horses leg was severe enough to necessitate putting the animal to sleep . When asked when the accident occurred the answer was simply over the weekend. Mrs . Rugheimer said that the gate adjacent to and across the entrance road near the control house was closed but twisted. She corrected the twisted gate upon it ' s discovery. Ron Portnell, employed by the City of Bozeman water department told me he had a dark brown elderly mare limping on Friday. Also he observed blood stained hoof prints near the bypass overflow outlet . Glen Stensrud and myself inspected the gates and fences that form the border of the North Hills Ranch and property owned by the City of Bozeman, and found no signs of blood, hair or any kind of struggle . The cause of the incident remains unknown and Mrs . Rugheimer has not indicated that personal involved with the Lyman Creek Water System were negligent or responisible for the injury. Julian Dodge � 0 :1 :; +. a En « ineers Lan d S �. r �.- ;; s �� �Z Sii�rr Bow t uuu. I'> A�' t;ra^i1�. .,:: . .rv�i y' ilk WEEKLY REPORT W.O. #86-511-1 LYMAN CREEK WATER SYSTEM IMPROVEMENTS May 22 through May 25, 1989 Nelcon Inc. worked four days this week may 22 through may 25 , 1989. The 16" D .I .P . water line was installed from Sta. 25+00 to Sta 38+37 and Sta 54+60 to Sta 61+05 for 1940 LF . Three 1110 bends , one 16" plug, on 16"xl6"xl6" tee, and one 16"xl6"x6" tee were mechanically attached .to the 16" waterline. Trench backfill was placed and compacted except over the tees . On May 24 Lyman Creek was diverted upstream from the proposed diversion dike at Sta 61+00. A ditch was excavated around Sta 61+00 and Lyman Creek was diverted into this ditch to allow for construction activities in the area. The foundation for the chlorine building was excavated on may 22 and the footings were formed and concrete placed on may 23, 1989 . Conditions on the project were generally dry throughout the week . Julian Dodge �... .) n s :,I I t I n 17 L 'l I T I p L I 5 Z-, L N'>. Boy SM. MO \ -.I: 'aa, lir.,n,!i. \I :u ~!i:,a >6'1.,i Si%Qr & a +/'—'1VT11� f • yam Ys. WEEKLY REPORT W . O . #86-511 -1 LYMAN CREEK WATER SYSTEM IMPROVEMENTS May 22 through May 25 , 1989 Nelcon Inc . worked four days this week may 22 through may 25 , 1989 . The 16 " D . I . P . water line was installed from Sta . 25+00 to Sta 38+37 and Sta 54+60 to Sta 61+05 for 1940 LF . Three 111/4" bends , one 16 " plug , on 16 "x16 "x16 " tee , and one 16 "x16 "x6 " tee were mechanically attached to the 16 " waterline . Trench backfill was placed and compacted except over the tees . On May 24 Lyman Creek was diverted upstream from the proposed diversion dike at Sta 61+00 . A ditch was excavated around Sta 61+00 and Lyman Creek was diverted into this ditch to allow for construction activities in the area . The foundation for the chlorine building was excavated on may 22 and the footings were formed and concrete placed on may 23 , 1989 . Conditions on the project were generally dry throughout the week . Julian Dodge C O 11 s LI i I it s L 7 a :i d S Li i e v r i sAN REM, P.0 Boy tnl. _`?ii �' _ • 'r.� . Bwn nl mn AI"!' C:nur. _. A� Grano.. .,,..,_. '.IT j,;0; -Ion) S/S/G &ENGINEERING SURVEYING A Consulting Engineers and Land Surveyors P.O. Box 861 W' 2010 North 7th Avenue Bozeman, Montana 59715 (406) 586-0588 WEEKLY REPORT W .O . #86 -511 -1 LYMAN CREEK WATER SYSTEM IMPROVEMENTS May 15 through May 18 , 1989 Nelcon Inc , worked four days this week May 15 through May 18 , 1989 . Installation of the 16 " D . I . P . water line was performed fron Sta 12+80 to Sta 25+00 for 1220 LF . Two 111/4' bends , three 221/2 ' bends , one 106 " x16 " xl6 " Tee and one 16 "x16 "x12 " Tee were mechanically attached . to the 16 " water line . At the 16 "x16 "x12 " Tee a 12 " plastic pipe was run over to the existing diversion as a portion of Change Order #1 . At the existing diversion the 12 " pipe was grouted to an existing 15 " clay tile pipe . The pressure relief vault at at Sta 23+00 was not installed and 16 " water line was placed ahead . Trench backfill has been placed and compacted to Sta 24+50 . Thrust blocks were poured for three 221/2 ' bends . Conditions on the project site were extremely wet and muddy Monday and Tuesday . Wednesday the area started drying up but by Thursday the weather produced wet and muddy conditions again . Nelcon Inc did not work on Friday May 19 , 1989 . Julian Dodge S/S/G &ENGINEERING SURV A EYING Consulting Engineers and Land Surveyors P.O. Box 861 2010 North 7th Avenue Mr, Bozeman, Montana 59715 (406) 586-0588 LYMAN CREEK WATER SYSTEM IMPROVEMENTS WEEKLY REPORT W .O . m86-511 -1 May 8 through May 14 , 1989 Nelcon Inc . worked 4 days placing 16 " D . I . P . waterline this week , May 8 through May 11 . The waterline was excavated , placed with bedding material , and backfilled up to 16 " over the top of the pipe . This work was performed from Sta 0+00 to 12+80+ for a total of 1280 feet of pipe in place . Backfilling activities were performed on May 11 and 12 . The trench was backfilled to the elevation of the pioneered road from Sta 6+50 to Sta 12+75 . There is still more finishing work to be done in this area . The project was muddy and slippery Monday and Tuesday but dried out by Wednesday and Thursday . Conditions in the beginning of the week slowed the contractors production but improved by midweek . Friday the snow showers caused muddy , wet conditions to return . Julian Dodge � S/S/G & ENGINEERING SURVEYING Consulting Engineers and Land Surveyors P.O. Box 861 2010 North 7th Avenue Bozeman, Montana 59715 (406) 586-0588 WEEKLY REPORT W .O . #86-511 -1 LYMAN CREEK WATER SYSTEM IMPROVEMENTS May 1 through May 7 , 1989 Nelcon Inc . worked 4 days' this week May through May 4 , 1989 , pioneering for the access road and for construction of the pro - posed 16 ' D . I . P . water line was performed Monday May 1 and Tuesday may 2 from Sta 0+00 to Sta 60+75 . This work was performed by a Cat 235 Backhoe and a Cat D6C dozer . The brush , slash and trees removed during this pioneering operation was buried at various locations however , not all slash piles have been buried to date . This buring operation was performed on Tuesday May 2 and Wednesday May 3 , 1989 . - . . . On Thursday May 4 , 1989 the existing 18 " A . C . water line at Sta 0+00+ area was searched for and found . Equipment involved was the Cat 235 Backhoe also three Nelcon employees and the Superintendent Glen Stensrud . Two hours of exploration was used and in the p .m . an 18 " coupling adapter , 18 "x16 " reducer D . I . P . , 16 " spool D . I . P . and 16 " 111/4' bend were attached to the existing 18 " A . C . water line . The 18 " spool D . I . P . was not used and a plane end connec- tion was used between the 18 "x16 " reducer and the adapter coupling . Julian Dodge ti. 1> 1 V) t oaj tl o ' I q _ 1 U1 V I I u dCi 2 `•. kl Jill lI i I Jj VI IIIII III F - j. ON tRZ i �j al 1,�I --A I Q. oC I LQ it atli v Q ] al Q'i j b Ri 0 Bills 1111 SRI N � I I i I • � i Zj �Zi a � � j 4G: 1�� x; I rl I � � �i NI A:� N JI �°- �. ,..:_�, > ,... q�.. •s .y '^ •- w .fir.- 1 eJl y tu p I VI _ II _ 1-4 14 i o`i �� tii 21 QI L1 TI-t. i UI 14; 41 t'V �J -1 lki v fii v Q z p 1 ell �I �I i i 2• wI �; wi I Qi i i i JI I Z'Jj 1 �A l h a 99 N; �, J � �� N q SI �v� �Q QI vi �„! •�, I � I ad. ' .rkI 0111 w QjI I Z ej 0. 41 �z o 3j y 4 J - �: Lu i w! r -41 QI Hi Q O N rn • ! 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