HomeMy WebLinkAbout21 - Design Report - Lot 4 Block 2 Opportunity Subdivision (Town Pump 6) - Water WATER MAIN EXTENSION
DESIGN REPORT
FOR:
LOT 4 BLOCK 2
OPPORTUNITY SUBDIVISION
BOZEMAN, MT
Prepared By:
OtATA
MADISON . . 'caAr,Is G.
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ENGINEERING = 2 �E ,
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Madison Engineering
895 Technology Drive, Suite 203
Bozeman, MT 59718
(406) 586-0262
March 2021
OPPORTUNITY SUBDIVISION—LOT 4
WATER SYSTEM DESIGN REPORT
A. General
This design report will give an overview of the proposed short 8" water main extension for the
future development of Lot 4 Block 2 of the Opportunity Subdivision located on North I9th at
Kimberwicke Street. The report includes a description of the proposed water main extension and
design parameters. The proposed improvements are anticipated to be constructed during the
spring of 2021. Once the water main is constructed and approved, the main will become a part
of the City of Bozeman(COB) system.
This main will not be put into use until future development is reviewed and approved by the City
for Lot 4. It is being constructed only to be installed under a parking lot that will be paved for
the recently approved Town Pump 6 Lounge.
The following references were used in the preparation of this report:
a. COB Design Standards and Specifications Policy, 2017. Addendum#6
b. COB Modifications to Montana Public Works Standard Specifications (MPWSS).
c. WQB Circular No. 1
d. City of Bozeman Zoning Map and City of Bozeman Water Facility Plan
e. 2015 International Fire Code
B. Existing Water Supply
The proposed water main extension will be served from the existing COB water distribution
system in Kimberwicke. The following information regarding pressures of the existing system
obtained from the COB:
Hydrants 1953 & 1786 (N. 19th& Cattail St.)
Static Pressure: 96 psi
Pitot Pressure: 74 psi
Residual Pressure: 86 psi
Hydrant Discharge: 1,445 gpm during test, 2.5" port
Distribution Main Capacity—Fire flow at minimum residual pressure
Q,=Qc[(Ps—Pm)/(PS—p,)]0.54
Q,= 1,445[(96—20)/(96—86)]0.54
Q,=4,320 gpm at 20 psi
Qt= Hydrant Discharge During Test
Q,= Fire Flow at Minimum Residual Pressure
P5= Static Pressure
Pm = Minimum Residual Pressure
Pr = Residual Pressure
P,= Pitot Pressure
Opportunity Subdivision—Lot 4
Water Design Report
Page 1 of 3
C. Proposed Water System
The proposed water main extension will connect to an ext'g 8" stub in Kimberwicke and consists
of approximately 135 linear feet of Class 51 Ductile Iron Pipe and extend north into Lot 4. The
proposed main will be looped in the future with the future development of Lot 4.
The layout of the proposed water main meets the COB design criteria and will be centered within
a 30' wide water main easement. A gate valve will be installed at the connection point to the
existing main per City standards. A blow-off will be installed at the end of the line, that will be
extended in the future.
D. Capacity Analysis
A capacity analysis was performed on the proposed water main extension. The water main
extension has been designed to meet the maximum day demand plus fire flow during the peak
hour. The main will ultimately serve Lot 4 which is 7.4 acres and zoned B-2, community
business. The City's Design Standards does not specifically reference water usage for B-2 zoning
so we propose to use the Sanitary Sewer Design Criteria for evaluating the water usage.
Based on Table V-1 of the City's design standards, it is estimated a B-2 lot will produce 2,000
gpd of wastewater flow per acre. Based on this value, the 7.4 acres, at full build out, will have
an estimated wastewater discharge of 14,800 gal/day. Assuming wastewater usage is
comparable to water usage, this equates to an average daily water demand of 10.3 gpm (0.023
cfs).
In addition to the average daily demand, the water main extension must account for peak periods
of daily use. Peaking factors are applied to the demand and account for these peak periods in
daily use. The peaking factors used are maximum daily use and peak hour and are obtained from
the COB Design Standards. Table 1 shows the peaking factors and the resultant flows from
those factors applied to the average daily demand of 23 gpm.
TABLE 1
PEAKING FACTORS
Flow Designation Peaking Factor Flow (gpm)
Average Day Demand 1 10.3
Maximum Dav Demand 2.3 23.64
Maximum Hour Demand 3 30.83
The required fire flow for a Type V-B structure up to 13,400 sf structure is 3,000 gpm. Based on
a fire flow demand of 3,000 gpm and a maximum hour demand of 31 gpm, a maximum hour
flow of 3,031 gpm is required. However, a 75% reduction in fire flow is allowed when a
building is provided with an automatic sprinkler system, which all buildings developed on the B-
2 property will likely have. Based on the allowed reduction, the required fire flow is 750 gpm.
TABLE 2
Opportunity Subdivision—Lot 4
Water Design Report
Page 2 of 3
ANTICIPATED FLOWS
Flow Designation Residential Fire Demand Total Flow
Demand m m ( m)
Maximum Day 23.64 750 773.6
Maximum Hour 30.83 750 780.8
The total demand during maximum hour, including fire flow, is 780.8 gpm. A Hazen-Williams
"C"Factor of 130 was used in the pipe evaluation. The working residual water pressure shall not
be less than 20 psi at any point in the water distribution system under maximum day plus fire
flow. The velocity shall not exceed 15 feet per second through the main line.
Results
The analysis was performed based on a dead-end main. Flow analysis of the 8-inch D.I. pipe
with a C value of 130 can provide the required 780.8 gpm with a pressure drop of approximately
9 psi from 86 psi to 77 psi, well above the minimum of 20 psi. with a maximum pipe velocity is
5.38 ft/s.
Capacity analysis calculations outlining the capacity of the proposed 8-inch pipe is included in
the appendix of this report.
E. Conclusion
Based on this analysis, the proposed 8-inch and 12-inch water main extensions for the
development of the proposed Opportunity Subdivision provide adequate service to meet the peak
hour demand, irrigation demand, and fire flows for the development.
This project will require the approval of the City Engineer and MDEQ.
Appendix
1. Water Main Capacity Analysis
2. Hydrant Pressure/Flow Test
Opportunity Subdivision—Lot 4
Water Design Report
Page 3 of 3
1 � �
2 O 4 2 O
Shaping Our Future Together
CITY OF BOZEMAN
HYDRANT PRESSURE/FLOW REQUEST FORM
Date: 6/2/16
Location Hydrant# Static Pressure Pitot Pressure Residual Pressure
N. 19` /Cattail St. 1953 96 86
Cattail W. of N. 19th 1786 74
Requested By: Brianna Baker
Fax#
Nozzle Size Flowed: 2.5"
Done By: ES /CD
Comments: 1445 GPM
2360
I �% ♦ j •1954 Q 1101 1100 1099 • 1
04 CA-1Rj S 1416 1418 1169
1415 ,, 1261 1260
1414 1408 • I ♦
•
2694 1257�I,R 1258
1445 14" 1417 •1409 1262 _-
• I� ST 1259
5 ! 1338 1166 1757 \��I `'1170
1443 2364 23db • ¢ 1337 !1762 17,61
\�1436�� • • 1756 17591
0 2165 2000
436- ♦ \\, \1442 • • 1760 ♦2+I4 11 1
1439— ♦ I�
1838
14 3 J • 1441.1� "1"164 *CAT
f_ IL.ST 1953
165-71785--
1493
_ 1172
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